You searched for: “W1248”
| # | Name* SORT (↑) | First Names | Title | Rank | RAF Equivalent Rank | Service No. | Born | Nationality | Role | Awards | Air Force | Command | Unit | DateofIncident *See Note SORT (↑) | Aircraft | Type | Serial | Code | Victories (Fighters) | Base | Time | Mission | Incident | Fate | Commemorated | Photo (Click to Expand) | Referring Database | Notes | Links/Archive Reports |
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| 1 | Tooth | Frank | Sergeant | 1026790 | Bomb Aimer (Navigator) | RAFVR | Bomber Command | 102Sqn (Ceylon)![]() | 1942-09-01 | Halifax | II | W1248 | DY-O | Pocklington | 2329 | Saarbrucken | On the return flight the starboard outer engine failed due to a coolant leak. Although they had made it back to Yorkshire the remaining three engines failed before a landing could be made at Pocklington, and a forced landing was made in a field near Low Catton, to the S of Stamford Bridge at 05:30 and all on board survived. | Survived - Killed in Action 1 Oct 1942 | Some of the crew walked to nearby East Farm owned by Mr Fred Lane. It was found that at the time of this incident the pilot had a habit of flying with the revs on the engines higher than normally recommended, this, combined with the flight engineer having set the petrol cocks incorrectly supplying fuel to the working engines had resulted in the available fuel in the tanks selected running out. The pilot very capable and this incident did not detract from his flying for which he was later awarded the DFC. After assessment of the a/c it was deemed beyond repair although the engines were taken away for re-use or stripping down for spares 102 Sqn Halifax W1066 | ||||||||||
| 2 | Stinson | Harold Keith | Pilot Officer | J/8418 | 13 Jan 1922 | Canadian | Pilot | RCAF | Bomber Command | 102Sqn (Ceylon)![]() | 1942-09-01 | Halifax | II | W1248 | DY-O | Pocklington | 2329 | Saarbrucken | On the return flight the starboard outer engine failed due to a coolant leak. Although they had made it back to Yorkshire the remaining three engines failed before a landing could be made at Pocklington, and a forced landing was made in a field near Low Catton, to the S of Stamford Bridge at 05:30 and all on board survived. | Survived - Killed in Action 2 Feb 1945 | Some of the crew walked to nearby East Farm owned by Mr Fred Lane. It was found that at the time of this incident the pilot had a habit of flying with the revs on the engines higher than normally recommended, this, combined with the flight engineer having set the petrol cocks incorrectly supplying fuel to the working engines had resulted in the available fuel in the tanks selected running out. The pilot very capable and this incident did not detract from his flying for which he was later awarded the DFC. After assessment of the a/c it was deemed beyond repair although the engines were taken away for re-use or stripping down for spares 433 Sqn Lancaster NG 460 | ||||||||
| 3 | McMullan | William Austin | Sergeant | 1059198 | 1920 | Air Gunner | RAFVR | Bomber Command | 102Sqn (Ceylon)![]() | 1942-09-01 | Halifax | II | W1248 | DY-O | Pocklington | 2329 | Saarbrucken | On the return flight the starboard outer engine failed due to a coolant leak. Although they had made it back to Yorkshire the remaining three engines failed before a landing could be made at Pocklington, and a forced landing was made in a field near Low Catton, to the S of Stamford Bridge at 05:30 and all on board survived. | Survived - Killed in Action 17 Jan 1943 | Some of the crew walked to nearby East Farm owned by Mr Fred Lane. It was found that at the time of this incident the pilot had a habit of flying with the revs on the engines higher than normally recommended, this, combined with the flight engineer having set the petrol cocks incorrectly supplying fuel to the working engines had resulted in the available fuel in the tanks selected running out. The pilot very capable and this incident did not detract from his flying for which he was later awarded the DFC. After assessment of the a/c it was deemed beyond repair although the engines were taken away for re-use or stripping down for spares 35 Sqn Halifax W7886 | |||||||||
| 4 | McIntyre | George Andrew | Sergeant | 1197253 | 1907 | Navigator | RAFVR | Bomber Command | 102Sqn (Ceylon)![]() | 1942-09-01 | Halifax | II | W1248 | DY-O | Pocklington | 2329 | Saarbrucken | On the return flight the starboard outer engine failed due to a coolant leak. Although they had made it back to Yorkshire the remaining three engines failed before a landing could be made at Pocklington, and a forced landing was made in a field near Low Catton, to the S of Stamford Bridge at 05:30 and all on board survived. | Survived - Killed in Action 1 Oct 1942 | Some of the crew walked to nearby East Farm owned by Mr Fred Lane. It was found that at the time of this incident the pilot had a habit of flying with the revs on the engines higher than normally recommended, this, combined with the flight engineer having set the petrol cocks incorrectly supplying fuel to the working engines had resulted in the available fuel in the tanks selected running out. The pilot very capable and this incident did not detract from his flying for which he was later awarded the DFC. After assessment of the a/c it was deemed beyond repair although the engines were taken away for re-use or stripping down for spares 102 Sqn Halifax W1066 | |||||||||
| 5 | Hodson | Albert | Sergeant | 1023522 | Wireless Operator/Air Gunner | RAFVR | Bomber Command | 102Sqn (Ceylon)![]() | 1942-09-01 | Halifax | II | W1248 | DY-O | Pocklington | 2329 | Saarbrucken | On the return flight the starboard outer engine failed due to a coolant leak. Although they had made it back to Yorkshire the remaining three engines failed before a landing could be made at Pocklington, and a forced landing was made in a field near Low Catton, to the S of Stamford Bridge at 05:30 and all on board survived. | Survived - Died Feb 2007 | Some of the crew walked to nearby East Farm owned by Mr Fred Lane. It was found that at the time of this incident the pilot had a habit of flying with the revs on the engines higher than normally recommended, this, combined with the flight engineer having set the petrol cocks incorrectly supplying fuel to the working engines had resulted in the available fuel in the tanks selected running out. The pilot very capable and this incident did not detract from his flying for which he was later awarded the DFC. After assessment of the a/c it was deemed beyond repair although the engines were taken away for re-use or stripping down for spares | ||||||||||
| 6 | Brazier | Colin George Arthur | Sergeant | 310756 | Wireless Operator | RAFVR | Bomber Command | 102Sqn (Ceylon)![]() | 1942-09-01 | Halifax | II | W1248 | DY-O | Pocklington | 2329 | Saarbrucken | On the return flight the starboard outer engine failed due to a coolant leak. Although they had made it back to Yorkshire the remaining three engines failed before a landing could be made at Pocklington, and a forced landing was made in a field near Low Catton, to the S of Stamford Bridge at 05:30 and all on board survived. | Survived - Died Wolverhampton 2001. | Some of the crew walked to nearby East Farm owned by Mr Fred Lane. It was found that at the time of this incident the pilot had a habit of flying with the revs on the engines higher than normally recommended, this, combined with the flight engineer having set the petrol cocks incorrectly supplying fuel to the working engines had resulted in the available fuel in the tanks selected running out. The pilot very capable and this incident did not detract from his flying for which he was later awarded the DFC. After assessment of the a/c it was deemed beyond repair although the engines were taken away for re-use or stripping down for spares | ||||||||||
| 7 | Bailey | Arthur Wilfred | Sergeant | 747748 | 1921 | Flight Engineer | RAFVR | Bomber Command | 102Sqn (Ceylon)![]() | 1942-09-01 | Halifax | II | W1248 | DY-O | Pocklington | 2329 | Saarbrucken | On the return flight the starboard outer engine failed due to a coolant leak. Although they had made it back to Yorkshire the remaining three engines failed before a landing could be made at Pocklington, and a forced landing was made in a field near Low Catton, to the S of Stamford Bridge at 05:30 and all on board survived | Killed on Active Service 7 Sep 1943 | Some of the crew walked to nearby East Farm owned by Mr Fred Lane. It was found that at the time of this incident the pilot had a habit of flying with the revs on the engines higher than normally recommended, this, combined with the flight engineer having set the petrol cocks incorrectly supplying fuel to the working engines had resulted in the available fuel in the tanks selected running out. The pilot very capable and this incident did not detract from his flying for which he was later awarded the DFC. After assessment of the a/c it was deemed beyond repair although the engines were taken away for re-use or stripping down for spares 1658 Conversion Unit Halifax DT524 |
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